BigSteve22
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So, I decided to try my hand at installing threaded inserts in the neck of my new Tele build. Results are fully functional, if not particularly pretty. Here's how it went...
First off, I used a cross slide vise mounted to my drill press so I could properly position the neck. Because the neck is tapered, it wouldn't clamp in the vise without some modification.
To offset the jaws to match the neck's taper, I used a few cardboard shims behind the jaw faces.
The vise itself was bolted to the drill press's work table.
I used an 1/8" twist drill bit, mounted backwards in the chuck, as an index pin to position the existing holes in alignment with the vertical axis of the quill. I used a square to check that the index was perpendicular to the plane of the mounting surface of the neck.
Once a mounting hole was in position, I used Forstner bits to drill a 3/8" Counter Bore, and then a 1/4" Blind Hole to accept the insert. I repeated the sequence of Index, Counter Bore, Drill, for each subsequent hole. Finally, I used a scrap of 80 grit abrasive paper wrapped around a 7/32" drill bit to slightly enlarge the the 1/4" holes. (That's because the actual bit size recommended by the insert manufacturer is 17/64", but I dare you to find a 17/64" Forstner bit!)
All went well, until the actual installation of the inserts. I used a piece of Red Oak to test the installation process. No problems what so ever, sucker went right in. So I figure: Hey, "I'm Golden". I put some Tap-Eze on the first inert, chucked the insertion tool in my trusty hand drill, and slowly started the installation. I soon realized that the Maple of the neck was a lot harder than the Oak, and that the only thing "Golden" was the shimmer of the soft brass insert. They went straight in, right up to the point where the slots cut into the rear of the insert's drive surface tore out! Thankfully, that was after clearing the plane of the mounting surface of the neck.
So, I ended up using a small grinding wheel in my Dremel tool to grind down the sharp edges left by the broken brass. As I said, they were already below the mounting surface of the neck, so no worries about functionality. (Yes, I did check after I was done!)
Thoughts for "Next Time"...
I realize that I left out one step that Kevin recommended: Use a 5/16-16 tap to thread the holes before installing the inserts. I only had the standard 5/16-18 on hand and I couldn't find an 16 pitch tap locally. Probably should have spent the money and ordered one. Oh well, maybe next time....
The body I have has a contoured heel, and I still have a couple of 8-32 x 1-1/2" screws left over from when Kevin worked on my JM neck. Now all I need to find is a couple of 1-3/4" S/S Oval Head machine screws. Next up, frets ends and check for level. Depending on how that works out, this neck might be making a trip to Detroit anyway.
:icon_jokercolor:
First off, I used a cross slide vise mounted to my drill press so I could properly position the neck. Because the neck is tapered, it wouldn't clamp in the vise without some modification.

To offset the jaws to match the neck's taper, I used a few cardboard shims behind the jaw faces.

The vise itself was bolted to the drill press's work table.

I used an 1/8" twist drill bit, mounted backwards in the chuck, as an index pin to position the existing holes in alignment with the vertical axis of the quill. I used a square to check that the index was perpendicular to the plane of the mounting surface of the neck.

Once a mounting hole was in position, I used Forstner bits to drill a 3/8" Counter Bore, and then a 1/4" Blind Hole to accept the insert. I repeated the sequence of Index, Counter Bore, Drill, for each subsequent hole. Finally, I used a scrap of 80 grit abrasive paper wrapped around a 7/32" drill bit to slightly enlarge the the 1/4" holes. (That's because the actual bit size recommended by the insert manufacturer is 17/64", but I dare you to find a 17/64" Forstner bit!)

All went well, until the actual installation of the inserts. I used a piece of Red Oak to test the installation process. No problems what so ever, sucker went right in. So I figure: Hey, "I'm Golden". I put some Tap-Eze on the first inert, chucked the insertion tool in my trusty hand drill, and slowly started the installation. I soon realized that the Maple of the neck was a lot harder than the Oak, and that the only thing "Golden" was the shimmer of the soft brass insert. They went straight in, right up to the point where the slots cut into the rear of the insert's drive surface tore out! Thankfully, that was after clearing the plane of the mounting surface of the neck.

So, I ended up using a small grinding wheel in my Dremel tool to grind down the sharp edges left by the broken brass. As I said, they were already below the mounting surface of the neck, so no worries about functionality. (Yes, I did check after I was done!)

Thoughts for "Next Time"...
I realize that I left out one step that Kevin recommended: Use a 5/16-16 tap to thread the holes before installing the inserts. I only had the standard 5/16-18 on hand and I couldn't find an 16 pitch tap locally. Probably should have spent the money and ordered one. Oh well, maybe next time....
The body I have has a contoured heel, and I still have a couple of 8-32 x 1-1/2" screws left over from when Kevin worked on my JM neck. Now all I need to find is a couple of 1-3/4" S/S Oval Head machine screws. Next up, frets ends and check for level. Depending on how that works out, this neck might be making a trip to Detroit anyway.
:icon_jokercolor: